2025-04-29
A large refinery operating a complex acid gas removal solvent was experiencing severe operational issues:
At the time, the refinery was using 10µm nominal polypropylene depth filters on the lean side (20% slipstream). These were proving ineffective in protecting the solvent loop from solid contamination.
Forensic Analysis: Root Cause of Filter Failure
IntegraLabs performed a destructive analysis on existing spent filters. The findings were clear:
Field Validation: Independent Testing by the Customer
To benchmark system performance, the refinery conducted its own solids sampling upstream and downstream of the filters:
Sample Location | Solids (mg/l) |
Upstream | 166.0 |
Downstream | 56.0 |
This revealed a removal efficiency of less than 75%, validating the lab findings and confirming a need for improvement.
The Jonell Solution: Pleated Cotton Cartridge Upgrade
Jonell proposed a pleated cotton filter cartridge featuring:
The new filters were installed and run for 5 weeks—more than double the service life of the original setup.
Updated solids analysis:
Sample Location | Solids (mg/l) |
Upstream | 130.0 |
Downstream | 4.0 |
Efficiency exceeded 90%, with dramatically cleaner effluent and no evidence of media degradation.
Key Results
Takeaway
This case underscores the value of filter media selection matched to process conditions. Jonell Systems’ combination of field support and lab analysis not only diagnosed the problem but enabled a validated, plug-and-play upgrade—saving the refinery time, money, and solvent.
Want similar results? Contact Jonell Systems to schedule a contaminant analysis or filtration audit. We’ll help ensure your filter media is precisely